STOUGHTON, Sask. –The Saskatchewan government says it has confirmed which pipeline leaked 200,000 litres of crude oil on First Nation farmland.
It says it belongs to Calgary-based Tundra Energy Marketing Ltd.
The company has been leading cleanup of the spill near Stoughton in southeastern Saskatchewan.
The government says so far 174,000 litres of oil have been recovered and 185,000 cubic metres of contaminated soil removed.
It says further assessment and cleanup, including excavation work, will follow until the site is restored.
Tundra confirmed on its website that it is the operator of the pipeline and is working with regulatory bodies and the Ocean Man First Nation to determine the cause.
Chief Connie Big Eagle said a band member who worked in the oil industry detected the smell of oil days before the leak was discovered.
The member eventually found the site of the spill contained in a small slough and reported it to officials on Friday.
She said emotions among the 540 band members range from disappointment to anger.
“Many of our people grew up in the oil industry and have made their careers in the oil industry and currently work in the oil industry, so there’s lots of knowledge,” she said in an interview Tuesday.
“I don’t know about things returning to normal, as far as the environment goes, but I know we’re all co-operating at this point, ensuring it’s cleaned up properly and no further damage is caused to the land or the environment.”
Tundra has said it immediately notified government officials and residents when the leak was reported and began removing surface oil with vacuum trucks.
Tundra is a subsidiary of grain and energy conglomerate James Richardson & Sons, Ltd., of Winnipeg.
The Ocean Man spill is almost as big as a 225,000-litre leak of heavy crude oil and diluent from a Husky Energy (TSX:HSE) pipeline into the North Saskatchewan River last July.
The leak forced the cities of North Battleford, Prince Albert and Melfort to shut off their water intakes from the river and find other water sources for almost two months.
Husky said it spent about $90 million responding to the spill, which it said was caused by shifting ground.